Release Note
C0FE002F_xxxx.sff
MPI Version
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FPGA Version
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03.03.00
Production Release |
C0FE002F_0346 |
03.02.00
Production Release |
C0FE002F_0345 |
03.01.01 |
C0FE002F_0311 |
03.01.00
Production Release
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C0FE002F_0311
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C0FE002F_0346
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Modications to gpioPinConfigReg |
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Reference Number: FP 336 |
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Type: General Change |
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FPGA Version: 0x0346 |
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Problem/Cause:
Prior to FPGA version x0346, gpio pins that were configured as an "output" did not resume "output" direction after an ioAbort event. Also, during the ioAbort event, if a service channel write to the gpio configuration register occurred, the gpio "output" pins would be set to "output" mode momentarily (and then cleared to "input" mode by the ioAbort event). After the ioAbort event was cleared, the gpio pin state would remain as in "input" mode unless software restored the gpio configuration register again. |
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Fix/Solution:
In FPGA version x0346 and later, an ioAbort event still forces gpio "output" pins to "input" mode, which allows external resistors to pull pins from either high or low for a "safe" state. The resistors may or may not be present depending on the PCB assembly. However, during an ioAbort event, service writes to the gpio configuration register no longer cause momentary "output" direction. After the ioAbort event is cleared, gpio pins will resume their previous "output" state without software intervention.
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Intermittent Dual String Discovery Failure |
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Reference Number: FP 332 |
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Type: Bug Fix |
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FPGA Version: 0x0346 |
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Problem/Cause:
Probe, resetRequest, and resetComplete were repeated on the wrong port (OUT port) when using the OUT port as the primary port during SynqNet node discovery. As a result, SynqNet node discovery may have failed. This problem was caused by the probe, resetRequest, and resetComplete being repeated on the wrong port. This issue existed in all FPGA versions prior to x0346. |
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Fix/Solution:
The FPGA code was corrected in version x0346 and later releases. This fix is required for systems using the Dual String or IN Port String topologies. This fix is NOT required for systems using normal OUT Port String or Ring topologies.
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sqMac - 0x00 will be read for dataType NULL |
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Reference Number: FP 323 |
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Type: New Feature |
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FPGA Version: 0x0346 |
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Description:
0x00 will be read for dataType NULL in the status and feedback packets.
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Intermittent Fault Recovery failures |
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Reference Number: FP 315 |
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Type: Bug Fix |
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FPGA Version: 0x0346 |
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Problem/Cause:
Some nodes may have intermittently failed to recover from a fault in some network configurations. If a node failed to recover, it exited cyclic operation and correctly triggered ioAbort logic (forcing outputs into "safe" states). Any nodes "downstream" of the failing node (after it switched ports) were also likely to exit cyclic operation. For any given node, there was only a small schedule window where this error may have occurred. There were two causes of the problem. The rcvMiiBuffer did not clear itself after an overflow in some situations. Also, a packet fragment generated by the fault recovery that happened to have valid CRC (but no data) would confuse the packetFifo, and corrupt internal node configuration bits. The first issue existed in FPGA build versions x0341 through x0345 and their branches (MPI release 03.02.00). The second issue existed in all FPGA versions prior to x0346. |
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Fix/Solution:
The fault recovery problems was corrected in FPGA build versions x0346 and later. The rcvMiiBuffer will correctly clear itself after an overflow. The xmitMiiReg will release xmitHoldRcvBuf within 8 clocks after a fault, preventing an rcvMiiBuffer overflow. 8 clocks will guarantee that there is minimum packet spacing between the packets. sqPll will ignore the second SYNQ packet after fault recovery (in case packet delays were effected in the cycle where fault recovery occurred). The rcvMii will correctly handle a valid packet with data length of 0. No software changes are required.
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C0FE002F_0345
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Pulse count sample problem with missed packets |
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Reference Number: FP 291 |
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Type: Bug Fix |
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FPGA Version: 0x0345 |
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Problem/Cause:
The pulse engine (step/direction logic) may appear to have a momentary position error after network packet errors (or fault recovery). The FPGA pulseFeedback value was not updated when DEMAND packet errors occurred. The "old" pulseFeedback value was sent back to the controller until valid DEMAND packets arrived, which may look like zero velocity to the controller. If a fault recovery is in progress, and the controller does not receive the FEEDBACK packet, the controller will interpolate the expected position based on constant velocity, then at the end of recovery, the controller may get one FEEDBACK packet with "old" pulseFeedback position (correct pulseFeedback will arrive in subsequent packets). This issue existed in all FPGAs prior to version x0345.
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Fix/Solution:
The FPGA code was corrected in versions x0345 and later. No software changes are required. |
C0FE002F_0341
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sqMac rxMiiBuffer multiple packets |
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Reference Number: FP 263 |
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Type: General Change |
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FPGA Version: 0x0341 |
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Description:
Add support for multiple packets to the rxMiiBuffer. This improves tolerance to network jitter. Prior to version x0341, the rxMiiBuffer could absorb up to 32 clocks (1.28 µS) of delay for a single packet, but only 8 clocks for multiple packets with minimum spacing. This change is required to meet theoretical worst-case network jitter in large networks (32 nodes). The improvement may also help at network startup, since the node's PLL phase error is larger than normal (as the PLL pulls into nominal lock). No software changes are required.
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sqNode adcAd977 double buffer |
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Reference Number: FP 260 |
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Type: General Change |
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FPGA Version: 0x0341 |
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Description:
Add double-buffering to the ADC input data. This change eliminates the need for a SynqNet scheduling limit (and the corresponding software error check). Prior to version x0341, a software error check prevented operation if the controller cycle time was less than the time required to complete the full ADC read sequence of all enabled channels. Otherwise, there would be a chance that packet data might be sent while new ADC data was arriving. This might result in some data from the "new" ADC read, and some data from the "old" (previous) read. If one 16-bit ADC value contained 8 bits of "old" and 8 bits of "new" data, this could cause an invalid value. For version x0341 and later, the ADC read data is double-buffered to prevent the possibility of bad data. If the controller cycle is faster than the ADC cycle, the node will send "old" data in multiple packets while the ADC cycle completes, then switch to "new" data.
NOTE: For existing systems, with controller cycles longer than ADC cycles, there is no change in ADC behavior. However, for new systems (with new MPI releases) it is possible to use higher controller rates without reducing the number of enabled ADC channels.
New FPGAs (x0341 and later) are fully backwards compatible with old MPI software releases. New MPI releases (starting with 03.02.xx) are generally compatible with old FPGAs (prior to version x0341). However, the former error check for ADC cycle period has been eliminated, so it is possible to configure a controller cycle rate fast enough to cause a problem when using old FPGAs with new MPI.
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C0FE002F_0340
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New BranchRev Register |
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Reference Number: FP 231 |
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Type: New Feature |
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FPGA Version: 0x0340 |
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Description:
Add BranchRev register. This extends the existing 16 bits of FPGA version number with 8 bits of branch and 8 bits of revision ID.
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C0FE002F_0311
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dedicatedIo - Expansion of dedicatedIn to 32 bits |
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Reference Number: FP 167 |
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Type: General Change |
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FPGA Version: 0x0311 |
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Description:
Expand the dedicatedIn word from 16 bits to 32 bits and add the status bits Feedback 0 Fault and Feedback 1 Fault. Note: Although the FPGAs now supports additional bits, the MPI does not yet enable them. |
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Clearing driveWatchdogFault and driveChecksumError |
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Reference Number: FP 160 |
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Type: Bug Fix |
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FPGA Version: 0x0311 |
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Problem/Cause:
Clearing the driveWatchdogFault and driveChecksumError required two service comandsa write to start the clear, and a write to end the clear. MPI releases prior to the 03.01.00 did not clear the bits.
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Fix/Solution:
Corrected the Drive Watchdog Fault and Drive Checksum Error bits to clear with a single service command. MPI releases 03.01.00 and later support this new behavior and clear the bits after a network reset. |
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Set unused pin default to FLOAT |
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Reference Number: FP 155 |
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Type: General Change |
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FPGA Version: 0x0311 |
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Description:
Set unused pins to FLOAT after the FPGA configuration process. After a power-on, but prior to FPGA configuration, SynqNet FPGA pins should be high-impedance outputs.
NOTE: The mode pins can enable internal pullups, but this is not recommended for SynqNet.
After configuration, unused pins will be high-impedance outputs with no internal pull-up or pulldown. In earlier versions, unused pins would default to weak internal pulldowns. This was not ideal since it could have conflicted with an external pull-up. |
C0FE002F_0303
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SqMax Cyclic Status |
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Reference Number: FP 141 |
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Type: Bug Fix |
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FPGA Version: 0x0303 |
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Problem/Cause:
There was a problem where SqMax NodeStatus cyclic status bits may have been corrupted after reading some of the FPGA registers (via the service command). The bits that could have been corrupted are: analogPowerFault, ioAbort, nodeAlarm, and nodeDisable. This issue has existed since release x0100.
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Fix/Solution:
This problem has been fixed. |
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Support for Multi-Vendor Flash Download |
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Reference Number: FP 140 |
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Type: General Change |
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FPGA Version: 0x0303 |
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Description:
Support has been added for a number of different flash component vendors. Flash components that are currently supported are:
Vendor |
PN |
Size |
Circuit |
Atmel |
AT25F2048N-10SI-2.7 (2MB) |
2MB |
Bowsprit |
Atmel |
AT45DB021B |
2MB |
Bowsprit |
Atmel |
AT45DB041B |
4MB |
Bowsprit |
Atmel |
AT45DB081B |
8MB |
Bowsprit |
NEXFLASH |
NX25P20-VN |
2MB |
Bowsprit |
NEXFLASH |
NX25P40-VN |
4MB |
Bowsprit |
SST |
SST25VF020-20-4C-SA |
2MB |
Bowsprit |
SST |
SST25VF040-20-4C-SA |
4MB |
Bowsprit |
STM |
M25P20-VMN6T |
2MB |
Bowsprit |
STM |
M25P40-VMN6T |
4MB |
Bowsprit |
STM |
M25P80-VMN6T |
8MB |
Bowsprit |
Xilinx |
XC18V02 |
2MB |
Outrigger |
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NodeDisable and analogPowerFault invert |
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Reference Number: FP 139 |
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Type: Bug Fix |
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FPGA Version: 0x0303 |
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Problem/Cause:
There was a problem with the inverted polarity option for the FPGA inputs nodeDisable and analogPowerFault. Prior to this fix, only the default polarity was functional. The problem happened because the hardware invert logic was inserted after the hardware latch function. Therefore, when "invert" was selected, the input would typically latch the negated state, and would not report a fault unless the latch was cleared by a software command. If the "invert" option was NOT used, the input would function correctly. This issue did not exist until the x020C release, where these inputs were first latched.
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Fix/Solution:
This problem has been fixed. |
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PhaseAdjust clash |
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Reference Number: FP 137 |
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Type: Bug Fix |
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FPGA Version: 0x0303 |
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Problem/Cause:
There was a problem in the sqPll function of the sqMac. With certain timing values, one node in the network may have fail to hold lock and then aborts cyclic operation. For a typical 3-node network, this timing typically occurred with TxTime set to 95%. Other TxTime values may fail in other network configurations.
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Fix/Solution:
This problem has been fixed. |
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24mA drive for GPIO pins |
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Reference Number: FP 134 |
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Type: General Change |
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FPGA Version: 0x0303 |
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Description:
The drive current of GPIO pins has been increased to +/-24mA. Other outputs which may drive opto isolators (LED outputs, nodeAlarm, ampEnable, brakeApplied) were already configured for 24mA drive current. See individual FPGA specifications for complete details of I/O characteristics. |
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SqMax rcvDataUnload |
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Reference Number: FP 123 |
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Type: Bug Fix |
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FPGA Version: 0x0303 |
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Problem/Cause:
There was a problem in the receive data unload function of the sqMax. In certain situations where the packet size did not match the configured packet size, invalid sqMax outputs were observed to cause "glitches" in the I/O output signals. The glitches would occur at the transition from cyclic to asynq operation, but the ioAbort signal would normally prevent these glitches from reaching external logic.
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Fix/Solution:
This problem has been fixed. |
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Improved Secondary Encoder Support |
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Reference Number: FP 109 |
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Type: General Change |
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FPGA Version: 0x0303 |
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Description:
Improvements have been made to the secondary encoder features. These changes allow the use of encoder faults and capture with secondary encoders. Secondary feedback for drives has also been added. The changes are NOT backwards compatible with software releases prior to 20031222 (secondary encoder feedback is not fully functional with prior software). |
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Improved ADC Support |
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Reference Number: FP 108 |
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Type: General Change |
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FPGA Version: 0x0303 |
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Description:
Improvements have been made to the ADC features to use the new "nodeIo" conventions. These changes allow up to 8 ADC channels per node (prior to this, the default was 1 ADC channel per motor). The changes are NOT backwards compatible with software releases prior to 20031222 (ADCs are not functional with prior software). |
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